To be presented at: V SEPOPE
Recife, Brasil
19 May, 1996
ITAIPU HVDC TRANSMISSION SYSTEM
10 YEARS OPERATIONAL EXPERIENCE
A. PRAÇA
H. ARAKAKI
S. R. ALVES
K. ERIKSSON
FURNAS Centrais Elétricas
J. GRAHAM
G. BILEDT
ABB Power Systems
Brazil
Sweden
ABSTRACT
Figure 1 is a simplified one-line diagram showing the
interconnection of the Itaipu power plant with
South/Southeast Brazil through the FURNAS
transmission system.
This paper describes the experiences of the Itaipu
HVDC system during the first ten years of operation.
The present use of the transmission and the system
dynamic performance is discussed, together with
significant events and availability performance.
The Itaipu power plant is a Brazilian Paraguayan joint
venture with a total installed capacity of 12,600 MW,
the majority of which is transmitted to Southeastern
Brazil, that is about 28% of the total system capacity.
Due to the difference in frequencies of the two
countries, half of the generation is at 50 Hz
(Paraguay) and half at 60 Hz (Brazil).
Ivaiporã
765 kV
Itaberá
765 kV
T. Preto
765 kV 500 kV
9 x700MW
units
345 kV
Itaipu
60 Hz
SOUTH
SYSTEM
Key words: Power transmission, HVDC, Itaipu,
1. INTRODUCTION
Foz
500 kV 765 kV
Itaipu
Foz
500 kV
500 kV
9 x700MW
units
Bipole 1
+/- 600 kV
Bipole 2
+/- 600 kV
Ibiúna
345
kV
2
Southeaster n System
The Itaipu HVDC system has now transmitted power
for 10 years. The scheme, designed in 1979, includes
many features new at the time and continues to be the
largest HVDC transmission, in both rating,
6,300 MW, and voltage, ± 600 kV. Major operating
features, present use, significant experiences and
availability performance are discussed. Since final
commissioning it has shown excellent performance
with a forced outage unavailability below half a
percent.
Itaipu
50 Hz
Paraguayan
System
Figure 1.
Simplified diagram of the
Itaipu Transmission System
Studies indicated a hybrid solution for the power
transmission, the power from the 60 Hz generators
transmitted by AC lines via intermediate stations and
the power from the 50 Hz generators transmitted by
an HVDC system.
2. THE USE OF THE HVDC TRANSMISSION
The Itaipu 60 Hz 765 kV HVAC transmission system
is operating over two series compensated lines with
the aid of a digital emergency control scheme (ECS)
to match generation and transmission capability in
case of disturbances in the electrical system.
The integrated system of South-Southeastern Brazil
had a peak demand of 33,700 MW and an annual load
of 210 TWh in 1994. Of this 35.5 TWh was supplied
from the Itaipu 50 Hz machines, over the HVDC
system.
For the 6,300 MW HVDC transmission, detailed
studies, including firm bid prices for the converter
stations, showed ± 600 kV to be the optimum voltage.
The subsequent performance confirms this choice of
±600 kV, with the attendant economical advantages.
The two bipoles are designed to operate
independently of one another under normal
conditions. Figure 2 gives an outline of the main
circuit, including the staged construction of the
HVDC transmission.
Figure 3 shows the monthly transmitted energy and
the peak power since 1991, the first full year of
commercial operation for the complete system. The
Actual Energy and Power Limits (AEPL) are the rated
power limits minus the power of the generators not
available; normally one machine is in maintenance.
The Expected Energy Use (EEU) is AEPL times 0.65,
the hydrological capacity factor.
Ibiúna
345 kV
1
Stage 3
sc
1
Stage 1
sc
2
2
sc
3
3
Stage 1
Stage 1
sc
4
to Guarulhos
Stage 4
5
to Interlagos
Stage 6 Foz
6
Stage 6
to Campinas
7
Stage 4
to T.Preto
8
Southeastern system
Stage 2
4
6000
5000
3,5
3
EEU
4000
2,5
3000
2
ENERGY
1,5
2000
1
1000
0
0
Stage 4
Figure 2.
AEPL
0,5
9
Itaipu
500 kV
PEAK
POWER
4
Energy - TWh/month
Foz
220 kV
0
Stage 5
1991 1992
1993
1994 1995
500 kV
Itaipu HVDC System main
circuit and evolution
Figure 3:
.
The stations are connected over two bipolar
transmission lines each approximately 800 km in
length, which follow separate rights of way, at least
10 km apart, except at the approaches to the stations.
Either transmission line can carry the rated output of
the station using the facility of parallel operation.
It can be seen from figure 3 that the actual transmitted
energy in most years has exceeded the expected
energy usage. This is due the considerations used
when deciding the energy dispatch in the Itaipu 50 Hz
power plant, that is:
-
The first stage was put into commercial operation in
November 1984 and the last commissioning activities
were completed in September 1990.
-
The Itaipu HVDC system is a landmark in HVDC
technology with regard to several features:
-
• Highest power rating and highest voltage, ± 600
kV
• A large step in converter rating, specially thyristor
and transformer
• The use of gapless Zn0 arresters
• Massive use of microprocessor-based controls
• Integrated factory system test of control equipment
Itaipu HVDC Transmission:
Monthly energy and peak power
-
-
Itaipu supply to Paraguay ranges from 100 to
500 MW.
The system spinning reserve contribution for
Itaipu is about 350 MW.
The South-Southeastern Brazilian electrical
system is 95% hydraulic.
Different hydrological conditions influence the
operation of the reservoirs. As an example the
rivers in the south region have relatively small
reservoirs.
From 1992 to 1994 there were excellent
hydrological conditions. The energy available was
much greater than the load.
When the hydrological conditions so allow, other
power plants closer to the load centers are chosen
to generate.
Peak power during each month - MW
TEPL
4,5
Paraguayan System
-
Since July 1994 the energy consumption in Brazil
has experienced a high rate of increase.
Figure 4. Control hierarchy structure
In practice, the microprocessor systems have proved
very reliable and more maintenance and interference
problems have been associated with the few hardware
systems than with the computer systems.
Additionally, the possibility to make fast changes,
plus debugging with an on-line monitor, makes these
systems much more convenient to use.
Thus the HVDC system is designed to operate over a
large range to meet the full load cycle, from peak load
on a work-day to about 25% capacity at weekend
light load. A routine of converter maneuvers, shunt
capacitor switching, filter switching and high Mvar
consumption is used frequently to fulfill the operative
requirements.
Due to these advantages microprocessor systems have
become accepted as the standard for HVDC controls
and although nowadays the systems are much more
powerful, with more on-line resources, Itaipu can be
seen as the first of this new generation of control
equipment.
3. CONTROL SYSTEMS - OPERATING
FEATURES AND EXPERIENCES
The control and protection systems for the HVDC are
almost completely based on microprocessor systems.
While this may not seem very remarkable today, at
the time of design, 1979, this was a very radical
decision. The control and protection systems are
based on an hierarchical design, see figure 4, starting
at the converter level, then pole, bipole and finally
station. The aim is that any failure, main-circuit or
control equipment, should reduce the transmission
capacity as little as possible.
In view of the rapid development in microprocessor
technology between 1979 and 1995, FURNAS is
considering upgrading the control and protection
systems, taking advantage of developments in the
latest generation of ABB equipment. The faster and
more powerful microprocessors allow an expressive
reduction in the number of components, permitting
complete digitalization and redundancy at pole,
converter and valve levels. Besides the increased
reliability and availability that could be achieved by
duplicating controls at converter and valve levels, a
significant reduction in routine maintenance work can
also be expected.
In general, the main control functions are carried out
using the ASEA DS-8 control system, based on the
Intel 8088 processor. This system provides for a large
quantity of I/O, both analog and digital, as well as
serial and parallel communication, being very suitable
for the tasks involved. Two control functions
requiring higher speed and accuracy, converter firing
control and the current control, use a system based on
the Intel 8086 processor with specially designed
hardware for the I/O functions.
3.1. MAN-MACHINE INTERFACE
The majority of the control actions are made by the
operators at the inverter station and only in special
cases is this done at the rectifier station. From the
regional dispatch center the following controls are
available: bipole power ramping; synchronous
compensator set point; AC filters maneuvers. The two
last features are normally used to control the voltage
at the 345 kV bus of Ibiúna.
At the pole and converter levels the equipment is not
duplicated, but a hardware back-up with limited
control possibilities is provided for the DS-8 systems.
At Bipole and Station levels the DS-8 systems are
duplicated, providing automatic transfer if necessary.
Station Level
AC system
control
Station control
desk
Foz: Itaipu generator station
SRQ: System operation centre
Bipole Level
Station Control
Bipole control
desk
Bipole 2
control
Pole
to other
station
to other
station
Tele Control
com.
Pole Level
Bipole 1
control
Bipole control
desk
Synchronous Power Control is the normal control
mode and it is only in this mode that all facilities are
available, i.e. overload, frequency control and so on.
The name Synchronous Power Control means that the
current controllers at both the rectifier and inverter are
synchronized; i.e., during ramping or other variations
in power order, the two are kept equal using the
telecommunication
system.
In
asynchronous
operation, the power or current order at both rectifier
and inverter must each be set by the operator.
Valve
Control
Convertor Level
convertor
control
3.2. AUTOMATIC CONTROL ACTIONS
The HVDC transmission represents a rather high
percentage both for 50 Hz and 60 Hz loads. Hence it
was necessary to include transient and dynamic
automatic controls to ensure the correct performance
of the integrated systems. These controls have to
attend the sometimes conflicting requirements of the
South/Southeastern Brazilian system and the
interconnected 50 Hz Itaipu/Paraguayan system.
To do that, additional power orders derived from
auxiliary controls are added to the order set by the
operators. The resulting value is checked against a
power order limit, being the minimum of a set of
limitations and an automatic value depending on the
number of 50 Hz generators in operation.
.
The main automatically initiated features are:
•
•
•
•
Stabilization of frequency in the rectifier end
Short-time Overload
Transfer of power between poles and bipoles
Reactive Power Modulation (Foreseen for SE
system stabilization, but now not required)
3.3. AC VOLTAGE CONTROL
The operators have the task of controlling the AC
system voltage, assisted by "Station Control", a
system that monitors the situation and gives
information, including minimum filter requirements,
maximum permitted filter at Foz and AC bus-voltage
control in Ibiúna, with high and low Mvar warning
set-points for the Synchronous Compensators.
At high loads, in addition to the need to supply more
reactive power to the converters, in Ibiúna there is
also a need to supply the network. This can be met by
adding filters above the minimum requirement and by
adding shunt capacitors. The four 300 Mvar
synchronous compensators are available for fine
control of the AC voltage. They are normally
operated with sufficient reserve capacity to cover a
single contingency failure, i.e. trip of a filter-bank or
loss of an AC line.
In Foz do Iguaçu there is a limit to the total capacity
of filters which may be connected, as a function of
number of generators, in order to avoid a potential
self-excitation situation. The generators are designed
with a 0.85 pu power-factor and consequently
contribute greatly to the reactive power balance.
At light loads in Ibiúna, the minimum filter
requirements may be such as to require other
measures to absorb reactive power. For this condition
High Mvar Control is provided where the inverter
firing angle is forced to increase, dropping the DC
system voltage and increasing the current. Hence the
reactive power absorbed by the converters is
increased. High Mvar Control has proved to be one of
the most useful additional facilities for the regulation
of the AC voltage, minimizing switching of filters and
capacitor banks and hence reducing maintenance of
circuit breakers.
3.4. PARALLEL OPERATION
For reasons of reliability, given the possibility of an
extended transmission line outage, the HVDC system
is equipped for parallel operation at both bipoles on
one bipolar transmission line. In one case when a
logging truck hit an HVDC tower, causing a
permanent bipolar outage, the repair of the line was
possible without any load shedding in the Brazilian
south/southeast system. In fact the transmission lines
have proven very reliable and parallel operation has
been used more for routine maintenance of both the
transmission line and the station line end equipment.
The actual sequences required to enter into parallel
operation are fully commanded from the station
control room in Ibiúna. In general all of the operator
controls used in normal operation are available in
parallel operation. From the operators' point of view
the power on the parallel poles is set in exactly the
same way as in normal operation, although the poles
obviously are part of different bipoles. Parallel
operation is permitted only at 600 kV, i.e. two
converters per pole. Reduced Voltage Operation may
be ordered by the line protection when in parallel
operation. Deparalleling may be ordered by protection
operation.
4. SYSTEM DYNAMIC EXPERIENCE
A Dynamic Performance Study (DPS) was performed
during the design stage and continued throughout the
commissioning as the various stages were put into operation. The fundamental objective was to
demonstrate that the transmission system would meet
the required performance as defined in the technical
specification. Exceptions to the specified performance
were sometimes found necessary to provide
satisfactory performance for the integrated networks.
Operational experience acquired since the start of operation, as well as the normal evolution of the AC networks resulting in a stronger inverter, indicate that
different dynamic performance is possible today.
Consequently FURNAS is in the process of revising
the dynamic performance study.
There are multiple objectives for the revised study:
• It is hoped that several control features, added to
achieve the specified performance can be removed
or simplified.
• Relaxing slightly the allowed levels of AC
harmonic distortion, (i.e. operation with less AC
filtering) more convenient reactive power control
may be possible.
• Introducing automatic power limits based on the
topology of the inverter AC network (runback
limiter) can maintain the inverter SCR at
acceptable levels during contingencies.
• Faster AC fault and commutation failure recoveries
can reduce frequency excursions in the sending end
AC system.
• Power modulation of the HVDC link may be
advantageous in enhancing the stability of the
FURNAS 765 kV AC transmission system.
The tools available to perform this study today have
also evolved compared with the early 1980’s. The
HVDC simulator, with its detailed DC controls,
continues to be essential. However a more complete
AC network representation is now available using the
RTDSTM (Real Time Digital Simulator) which is
interfaced with the HVDC Simulator.
5. SIGNIFICANT OPERATING EXPERIENCES
During these ten years of operation a considerable
number of interesting experiences have occurred,
especially during the first five years which were
concurrent with construction and commissioning. The
division of the work into stages which were
constructed and put into operation sequentially
followed the schedule for the generating units in
Itaipu and permitted continuous transmission of the
available energy. This simultaneous commissioning
and operation, while not restricting energy
transmission, can be seen in the higher forced outage
figures in the first years. This section will not try to
cover all events from these ten years, but concentrate
on the most significant items.
5.1. HARMONIC EXPERIENCE
The service experience, both with respect to level of
harmonics and to consequent interference, has shown
the performance to be well within specified
requirements.
5.1.1. AC side harmonics
The method of calculating the level of AC side
harmonics is very conservative. It takes into account a
range of possible resonances with the AC system as
well as worst case parameters, e.g. combinations of
tolerances in transformer impedances and unbalances
in firing angles.
In practice, these factors are not as bad as assumed
and the AC side harmonics are less than calculated,
especially for non-characteristic harmonics, and the
interference levels well within the specified levels.
One interesting factor is that a filter is included for the
non-characteristic third and fifth harmonics. This
filter was included for performance reasons, when
calculating with pessimistic assumptions. In actual
operation, it has been found that the loading of this
filter is well above the expected level. However, this
is due to fifth harmonic currents originating in the AC
network. The sources of these harmonics are diverse,
and at the moment not completely identified, but for
sure influenced by industrial loads and to a large
quantity of TV sets with single pulse rectifiers.
On a weekend and during a final match of the 1995
South America Football Cup, measurements taken at
the Ibiúna station demonstrated clearly the heavy
influence of TV sets on the fifth harmonics levels.
5.1.2. PLC harmonics
The technical specification gave very strict
requirements regarding PLC interference to reduce the
noise generated by the converter stations over the
frequency range 30-500 kHz. Theoretical calculations
indicated that this may not be met over the range 30120 kHz. However, in view of the potential cost
savings, it was agreed to postpone any decision on
PLC filters until measurements could be made on the
operating system.
As part of the final commissioning, measurements of
PLC noise were made at the coupling capacitors on
the AC lines. These measurements, made over the 30500 kHz range, showed that the noise somewhat
exceeded the specified level at frequencies below 100
kHz, but was acceptable, especially when considering
actual and proposed PLC frequencies. Accordingly, it
was decided not to install the PLC noise filters, see
reference 3.
5.2. FLASHOVERS ON 600 kV WALL
BUSHINGS
Operation with 600 kV started in July 1985 in the
negative pole of Bipole 1, with no apparent problems.
Less than 3 months later a flashover occurred on the
DC pole bushing at Foz do Iguaçu. The bushing was
checked, but no defect found. Pollution samples
showed a low level compared to those normally found
in connection with pollution flashovers. At the time
of the occurrence it had been raining heavily for about
half an hour.
By the end of the year, a total of five flashovers had
occurred at Foz do Iguaçu and two flashovers at
Ibiúna, on both the positive and negative poles for
five different bushings, all under heavy rain
conditions. By that time it had become clear that this
was a general problem for the 600 kV wall bushings
and full voltage tests had been started to determine
the reason for the flashovers. The tests were
supplemented with data collection from other sites
and comprehensive meteorological observations from
the Foz and Ibiúna stations.
It was confirmed that a rain shadow close to the wall
decreased the withstand voltage considerably, see
figure 5, and that the length of the dry zone was an
important parameter for withstand strength. A
minimum withstand dry zone could be found and
figures as low as 350 kV were recorded. Observations
at site established that a rain shadow gave a dry zone
on the bushings close to the wall. Later electrical field
measurements confirmed that a dry zone causes a
steep increase in the electric field and that this is the
cause
of
the
flashover.
flashovers. Thus, further work was concentrated to
these solutions.
RTV had shown good performance in other
installations and had indicated longer life-times than
silicone grease, but application is more difficult and it
is uncertain if it can be removed easily. During an
investigation on test specimens on site, RTV
exhibited an unexpectedly rapid loss of its
hydrophobic properties. This was followed up by
laboratory experiment that showed that if exposed to
water over a long time, RTV would lose its
hydrophobicity. Thus it seems that RTV may not be
efficient in tropical climates with heavy and abundant
rain. The conclusions were that silicone grease of the
type chosen could most probably get a lifetime of 4 to
5 years in a clean ambient atmosphere and that
thickness and evenness were not a problem. Even a
fairly thin layer would protect the hydrophobicity and
thereby prevent rain flashovers. This was confirmed
by an on site test program for various types of
silicone grease and RTV, including application to
energised test insulators at 600 kV. On the wall
bushings the time between exchanges was increased,
for the original grease type, under close supervision
of characteristics, especially hydrophobicity, see
figure 6.
Figure 5. Rain shadow
From the investigations it became evident that it was
necessary to either decrease the stresses over the dry
zone or increase its withstand capability. The most
promising method seemed to be to make the insulator
surface non-wetting and thereby decrease the steep
electrical field increase in the transition between the
wet and dry zones. This could be made by application
of a hydrophobic coating on the insulator surface by
silicone grease or room temperature vulcanized
silicone rubber (RTV).
In June 1986 silicone grease was applied to all 600
kV wall bushings as a temporary measure while the
investigations continued. Evaluation was made of
coated insulators, both compared to other possible
countermeasures and also between RTV and silicone
grease. No conclusive improvements could be found
from other measures such as alternative porcelains or
booster sheds. Both RTV and silicone grease seemed
to give considerable improvements and the
experiences from the temporary silicon grease
application was excellent, preventing further
Figure 6. Foz do Iguaçu 600 kV wall bushing.
Hydrophobicity test on silicone grease after 38
months exposure time.
Actual experience has shown that removal and
reapplication can be considerably facilitated by
control of the chemical composition and the use of
simple hand tools that were developed. Now, with
more than nine years successful use of silicone
grease, the procedures developed have led to fast and
well controlled grease renewal. A minimum four-year
lifetime is proven by operation experience for the
conditions prevailing at the Itaipu converter stations.
5.3. CONVERTER TRANSFORMERS
During the early years of operation significant
problems were experienced with the converter
transformers. This was distributed fairly evenly between the rectifier and the inverter and between
300 kV and 600 kV. The four types have the same
conceptual design, although they are not identical in
detail.
The first indications were given mid-1985, after about
six months of operation, when gas in oil analysis
showed gassing, at a low rate, in some transformers.
In October 1985 a failure occurred in one transformer
at the inverter station and was traced to the AC winding. Shortly after a second failure occurred in the
rectifier, located at the DC winding outlet. One of the
failed transformers had shown gassing, including
acetylene, while the other one did not show more gas
than had been generally expected.
The examination of the first failed unit, together with
inspections in another gassing unit, revealed bad
contacts between a copper plate and an aluminum
plate. This was evaluated as the cause of the gassing.
A program to modify the contacts was carried out
during early 1986.
After a few months operation, gas in oil was found
again in some modified transformers. In May 1986,
another transformer failed in the inverter, with the
failure in the AC winding. Special investigations were
undertaken at the factory and an extended heat run
test indicated that the gassing had its origin in
induced currents circulating in the core.
A second modification of all transformers to reduce
the induced currents was undertaken and again carried
out on site and in the workshop. The site modification
was carried out while the link was in commercial
operation and this meant that a considerable time
elapsed, even though extra spare units were delivered
to facilitate the execution of the work and to give
more security against service interruptions.
In 1989 the work to execute the modifications was
finalised. During this time further failures occurred,
some of which were after the second modification had
been completed.
A detailed analysis of the failures was presented in the
CIGRÉ 1993 Joint Task Force 12/14, 10-01 and will
not be repeated here. A summary is given below,
where it can be seen that the failures are concentrated
in the first years of a transformers operation.
Years of
Operation
0-1
Number of
Failures
6
1-2
2-3
3-4
4 -10
3
2
1
0
The failure rate for these converter transformers has
been higher than one would normally expect for this
type of equipment. This can be explained as due to a
large step in converter transformer development
especially with regard to unit rating, coupled with
severe transport restrictions. This resulted in a
relatively large number of new techniques which,
although extensive prototype testing was made, were
still not fully controlled during the manufacturing
process. However the last five years of operation
make us feel confident in the present and future
service performance of these transformers.
5.4. VALVE HALL FIRE
In May 1989 a fire broke out in Converter 5 at the
Foz do Iguaçu substation. This was due to an
unfortunate combination of circumstances which are
summarised here.
Information from personnel present at the time, plus
event recorder printouts and a detailed inspection
made in the valve hall, identified the following failure
sequence:
1. A water tube between two thyristor levels in valve
2, close to the top of phase A quadruple valve,
comes loose and water leaks at approximately 1 l/s
.
2. A water leakage alarm is emitted, however the
protection system does not trip as the trip signal is
inhibited due to an open by-pass valve.
3. Water flows down in quadruple valve A during at
least 8 minutes, corresponding to approximately
500 liters. The conductivity of the originally
deionized water increases when flowing over the
valve modules, due to contamination with the
small amounts of dust and dirt it picks up.
4. A flashover occurs in the bottom valve of phase A
and gives a short circuit across that.
5. The flashover strikes the damping capacitors in the
bottom valve of phase A and starts a fire in some.
6. The fire spreads upwards in the quadruple valve
structure where it increases in heat generating
capacity and intensity, so that aluminum and
plastics melt and porcelains crack.
7. The fire is discovered. The ventilation system is
closed and after some hours the fire has selfextinguished.
A full scale experiment in which the corresponding
water tube was cut open was made and the sequence
recorded. This confirmed that the trip signal was not
given due to the fact that the by-pass valve for rapid
refill was erroneously left in the open position.
Phase A quadruple valve was damaged by fire. The
other two quadruple valves were not directly damaged
by fire, but rather by smoke. A large amount of
hydrochlorides from burning plastic was precipitated
on all equipment. Due to this contamination the major
part of the equipment was replaced. Only the busbars
and some very special items were not manufactured
new. The valve hall was put back into operation in
slightly less than 14 months and entered into
operation in July 1990.
After the fire incident some modifications to the
system were introduced:
• A locking key on the by-pass valve for rapid refill
was installed to avoid operation of the thyristor
valves if this valve is left open.
• A new trip function was introduced, based on the
derivative of the water level.
• The start of the make-up pump was delayed 10
minutes in order to ensure operation of the low
water level trip at a leakage rate of more than 0.14
l/s.
• A new frequent make-up alarm was included.
• The Bipole II water connections between thyristor
levels were exchanged for the type used in Bipole
I, having a superior ferrule fixing.
Later a full scale test of incipient fire detectors was
made. Testing demonstrated the possibility to identify
a pre-combustion condition by detecting submicron
particles emitted from overheated plastic material.
The successful testing led to the decision of a full
scale installation of such detectors in all converters.
This installation was completed in August 1994.
5.5. VALVE COOLING SYSTEM
After several years of operation, discoloration was
noticed on the stainless steel pipe couplings used to
connect the fine water PEX pipes between modules.
In some converters actual corrosion of the tubes in
certain positions had taken place, but the process was
far from uniform and not necessarily worse in
converters having longer operating times. As this
effect occurred only at the anodic ends of the tubes a
process of electrolytic corrosion was suspected. In
fact the design allowed for some corrosion of the
tubes over a 50 year period, however in many cases a
faster effect was seen. This was the case even though
the water quality had been maintained at the low
levels of conductivity required to limit the stray
currents in the cooling water. A series of
investigations both in the laboratory and at site
determined that the foreseen electrolytic corrosion
was accelerated by the presence of free negative ions.
The origin of these ions was probably the water
treatment resins used on the system, the ions being
released at the time of exchange of resins.
There were several ways to resolve this situation,
however the chosen solution was to modify the
cooling water pipe couplings to make them resistant
to this phenomenon. In summary the stainless steel
pipe couplings were replaced by plastic couplings, in
which an inert electrode is utilised to ensure
satisfactory voltage distribution within the water
circuit. In addition to laboratory tests on the materials
used and thermo- mechanical life cycle testing on the
new couplings, a full scale dielectric test program was
carried out. Also finer water filters were introduced to
replace the original filters.
The work to change the pipe couplings and also to
clean the valves of corrosion products and possible
remaining catalytic agents was carried out during the
first half of 1994. The results of monitoring the
modified cooling system indicate that the solution
adopted is giving fully satisfactory performance.
5.6. MAINTENANCE
Preventive maintenance is an activity having a
significant influence on the system operation, both
from the point of view of manpower and
performance. In order to evaluate the impact of the
preventive maintenance activities on the availability
of the power transmission, a trial preventive
maintenance was performed. This determined the
duration to be used as a maximum for the availability
guarantee calculations.
This trial consisted of an actual maintenance at
Bipole, Pole and Converter levels of equipment for
which the shutdown has an impact on the power
transmission capacity. The activities to be carried out
were defined by the Preventive Maintenance Plans for
the substation and considered necessary for a good
performance of the HVDC system and were based on
the manufacturers recommendations, the previous
experiences of the converter station supplier and the
experience obtained by FURNAS in the operation of
the converter station.
At converter level, the preventive maintenance of the
By Pass Breaker was found to be time-consuming and
this equipment proved critical for the converter
outage time, much more than, for example, the
valves. At Pole level the HVDC Control and
Protection maintenance showed to be the most time
consuming equipment, as expected. Disconnecting
Switches, in spite of the large number, were
maintained in only 7 hours. At Bipole level both
Bipole Control and Protection and Common Yard
equipment were maintained in around one and a half
hour.
The evaluation of the times achieved during the trial
maintenance resulted in outage to be used for the
calculations of the Availability and Reliability
Guarantee (see Table 1).
LEVEL
Bipole
Pole
Converter
MAXIMUM OUTAGE TIMES
2 hours per year and per bipole
11 hours per year and per pole of which
2 hours overlapping with bipole outage
18 hours per year and converter of
which 11 hours overlapping with pole
outage
Table 1: Outage times to be used for AR Guarantee
In practice the preventive maintenance is planned
according to an annual time schedule, to a large
extent based on optimisation of manpower. Two
weeks before the maintenance, the central dispatch is
informed about the equipment that will be under
maintenance, so that all interconnected utilities can be
informed. However, if for some reason any equipment
is out of service, efforts are made to take advantage of
this and preventive maintenance is performed.
So far, taking into account the use of the HVDC
transmission, it has not been necessary to schedule
maintenance in the manner in which the trial
maintenance was performed. This is because it has
been possible to shut down converters, except in the
heavy load period, without prejudicing the power
transmission, allowing more time for maintenance
and reducing total maintenance staff and overtime.
Such a procedure reduces costs, although the system
availability decreases.
One interesting result of the maintenance activities is
the very low thyristor level failure rates found. This
has been consistently below 0.1% per year and in
1995 was 0.03%, that is three failures in more than
18 000 levels.
6. AVAILABILITY
Table 2 presents the availability of the Itaipu HVDC
transmission system in two different formats. One
according to CIGRÉ definitions and another
according to the contract for the supply of the
converter stations.
YEAR/
BIPOLE
88
89
BP1
BP2
BP1
UNAVAILABILITY
BY CIGRÉ (%)
Forced
Schedule
d
1.5
4.6
6.9
6.9
AVAILABILITY
(%)
CIGRÉ Contract
91.6
88.5
-
90
91
92
93
94
95
BP2
BP1
BP2
BP1
BP2
BP1
BP2
BP1
BP2
BP1
BP2
BP1
BP2
15.6
0.7
14.2
0.6
0.4
0.3
0.7
0.2
0.2
0.4
0.2
0.1
0.4
7.8
7.7
10.6
12.3
12.9
8.8
6.4
2.6
2.5
6.4
5.9
2.1
2.1
76.6
91.6
75.2
87.1
86.7
90.9
92.9
97.2
97.3
93.2
93.9
97.8
97.4
99.5
98.9
99.1
99.4
99.3
99.4
99.4
99.3
Table 2. Itaipu HVDC Transmission System Bipoles
Availability
It can be seen from that table that the contractual
figures do not match the reporting to CIGRÉ as the
two formats are different. The main difference
between the calculations is that the report to CIGRÉ
does not take into account the actual maintenance
procedures used at site, penalizing the availability
figures, while the contractual figures consider that the
maintenance could be performed, if necessary,
according to the trial maintenance results, see 5.6,
which corresponds to an equivalent unavailability of
0,28% per bipole and year.
Considering that scheduled maintenance is carried out
taking advantage of periods of low utilization, the
availability format used by CIGRÉ has been
questioned by many utilities, including Manitoba
Hydro and FURNAS, at the HVDC Users Conference
held last September, 1995 in Winnipeg, Canada.
Another difference between CIGRÉ and contractual
availability figures is that the contractual calculation
gives less than proportional weight to outage of a
converter than to outage of a complete pole,
considering the design with series connected
converters and the impact on power transmission of
having one converter out of operation. Also certain
type of events outside the contract such as DC line,
AC network and human errors are excluded from the
calculations based on the contract.
In table 2, the unavailability figures for Bipole 2 in
1989 and 1990 were affected by the valve hall fire.
The 1994 scheduled unavailability for both bipoles
reflect the outage time for installation of the incipient
fire detection systems mentioned in 5.4 and the
modification to the valve cooling circuits discussed in
5.5, which were carried out together, sequentially, in
all converters
Table 3 shows the main causes of disturbances for the
last eight years without giving weight to how large
part of a pole is affected. In that table all forced
outages for the two bipoles, with a total of eight
converters per station, are summarised. It can be seen
that there is a general trend for the annual number of
converter equipment forced outages to reduce with
time. The number of forced outages due to control
and protection is significant, especially in 1989 when
many were due to commissioning of the bipole
paralleling system together with commercial
operation. In recent years, there is a trend to decrease,
except for 1992 and 1993, when they were high.
These two years suffered from repetitive faults of
transient nature that were hard to trace. In particular
one fault in a pole current control amplifier and a
series of similar faults in the power supplies to the
valve control cubicles are responsible for most of the
control faults.
The weighting counts one pole as a single unit,
reducing the impact of converter outages to the
significance that they have on power transmission.
Many of the counted outages were in fact the same
failure, but the process of ”trouble shooting” could
have contributed to a further disturbance. This is
illustrated in Table 3 by the values in parentheses,
where the outages due to the same failure have been
discounted.
This illustrates the advantage that would be obtained
by the use of duplicated control equipment, which not
only avoids the outage, but also permits on-line fault
tracing, as well as routine maintenance. Such a system
would therefore increase the availability, both forced
outage and scheduled.
For the last four years the "equivalent weighted forced
outage per bipole" has been monitored. This value
excludes human errors and covers station equipment
only.
YEAR
DESCRIPTION
1988
1989
1990
1991
1992
1993
1994
1995
10
5
6
5
1(1)
4(3)
1
7(5)
CONTROL AND PROTECTION 22
60
29
5
23(16)
18(12)
9
9(7)
MAIN CIRCUIT EQUIPMENT
7
9
5
2(2)
4(4)
4
2
72
44
15
26(19)
26(19)
14
18
20
9
36
4
10
19
20
12
AC SYSTEM
2
3
-
-
-
-
-
-
HUMAN ERRORS
22
30
12
5
12
7
4
4
TOTAL
92
114
92
24
48(41)
52(45)
38
34
AUXILIARY SERVICES
TOTAL
EQUIPMENT
DC LINES
16
CONVERTER 48
EQUIVALENT
WEIGHTED
OUTAGE PER BIPOLE
Table 3. Itaipu HVDC transmission. Total forced outages
BP1/BP2 BP1/BP2 BP1/BP2 BP1/BP
5.8/4.5
2.5/3.8
5.8/4.5
2
1.5/4.0
The figures given for the dc line include transient
faults with successful restart. Many of the DC line
faults in 1990 were caused by flashovers to a
eucalyptus tree and in most cases the faults did not
cause a pole outage. The performance of the ± 600 kV
dc lines has proven to be very good. The two lines
use 30 insulators per suspension string, giving a
specific creepage of 27.7 mm/kV and have a total
length of over 1600 km. In the last three years there
have been a total of 51 faults, of which only 12 did
not restart with success. This gives an average of two
pole outages per bipole/year, which in general were
restarted manually without any problem.
7. CONCLUSION
The Itaipu HVDC Project, designed in 1979, includes
many features new at the time and continues to be the
largest HVDC transmission, in both rating,
6,300 MW, and voltage, ± 600 kV. During the now
more than ten years since first power transmission,
the system has operated continuously supplying a
major part of the Brazilian load, always providing
transmission capacity for the available generation.
The early years experienced significant challenges in
commissioning and operating the system, as one may
expect in such a large project. The final stage of the
project was fully commissioned in 1990, including
the use of parallel operation. In the last five years
since then, the average forced outage unavailability
has been below half a percent.
Figure 8. View of Foz do Iguaçu station
8. REFERENCES
1. V. Madzarevic, C.A.O. Peixoto, L. Hagloef:
“General Description and Principal Characteristics of
the Itaipu HVDC Transmission System” from
Conference Sharing the Brazilian Experience, Paper
1.1, Rio de Janeiro March 20-25, 1983
2. A.G Figueiredo, A. Praça, N.L. Shore: “Master
Control of the Itaipu HVDC Transmission System”
from Conference Sharing the Brazilian Experience,
Paper 1.7, Rio de Janeiro March 20-25, 1983.
3. Marly R. Bastos, Jose Torquato P. de Souza, John
Graham, “Interferencia das Conversoras de Corrente
Continua no PLC do Sistema de Corrente Alternada.”
XI SNPTEE, Rio de Janeiro, 1991.
4. W. Lampe, D. Wikström, B. Jacobsson: “Field
Distribution on an HVDC Wall Bushing during
Laboratory Rain Tests” IEEE 1991 WM. 125-5
PWRD.
5. “In-service performance of HVDC Converter
Transformers and Oil-cooled Smoothing Reactors”.
CIGRÉ Joint Task Force 12/14.10-01, 1993.
6. H. Arakaki, J. Lopes, A. Praça: “Itaipu HVDC
Transmission. System-Analysis of Control System
and Protection Performance after two years of
Operation”. Winnipeg, July 1987.
7. A. Farias, I. Oliveira, L. Correa et Al.: “Emergency
Control Scheme for the 765 kV AC Itaipu
Transmission System Using Logical Programmable
Controllers”. CIGRÉ Latin American Conference.
May 1995, Foz do Iguaçu, Brazil.
8. Delfim P. Amaral, A. M. de Freitas, John Graham.
”Implantaçâo de Sistema de Detecçâo de Incendio em
Valvulas Tiristoras - Experiencia de Furnas”
XIII SNPTEE, Florianopolis, Brazil, 1995.